Wednesday, 6 July 2016

Metal Forge / Induction heater

YouTube suggested I watch this video.. Grant Thompspn - "The King of Random"

Ooo, thats good I thought. I'll make one.  So I purchased some of the stuff to make this small charcoal fired forge, then remembered I was an electronics engineer and thought why am I not making an electric one?  I pondered this for a while and then thought why am I not building an induction heated forge.  So thats what I have started doing....

Induction heating involves inducing eddy currents in the work piece.  These currents are big, so the work piece heats up.

Wikipedia has the explanation here https://en.wikipedia.org/wiki/Induction_heating

The output stage of this heater will probably connect to rectified mains so I would like all the control electronics isolated from this.  I started with what I had 'in the drawer' to construct an oscillator and gate drive transformer driver.  The IR2153 is a self oscillating half bridge driver, so sounded ideal for what I was trying out.

IR2153 Half Bridge
The board is supplied with 24V for the half bridge, regulated down to 12V for the IR2153.  This provides a +/-12V square wave output to drive a gate drive transformer.

Out of curiosity I connected this...

...to the output of the driver via a 1uF Cap.  Using a 'scope I could tune the IR2153 to get the coil resonating.  This was able to heat my screwdriver up to above 100°C, I know this because my finger sizzled when I touched it.

From initial measurements on the above coil of wire I could tell the final coil would be conducting 100's of amps, so water cooling would be a good idea.  I got some 8mm copper tubing and found a paint tin to wrap it around.  I couldn't just wrap the tube around the tin, it would buckle at the first bend, so I perused the WWW and plenty of people suggested filling the tube with salt.  This I did and the tube bent very nicely...

...Getting that salt out was difficult and took ages, tap tap tap, rotate, tap tap tap, rotate, Zzzzz
I tried buzzing it out with a sander and all sorts.

I needed a smaller coil.  I wasn't going to use the salt method again.  Water doesn't compress, so I capped one end of tube with a compression fit stop end, filled the tube with water and capped the remaining end.  The tube requires a slight tweak to take up any air that got in, but after that the tube wrapped up into a coil nicely.  Getting the water out was easy, just release the compression fittings and empty the water out.  Using the compression fittings 'wastes' a couple of olives and some tube but saves a lot of time.

The coil gets hot without cooling, so I purchased a water CPU cooler from ebay.  It was 'untested', but after cleaning it out, removing pipework and re-piping it to the coil, it pumped water round no problem.

The pump and cooling fan required an extra 12V supply, the pump at 200mA and the fan at 1.5A.  I decided to under run the pump and fan at 10V and constructed a 2A buck regulator from a TL494 and associated components.

The heater as it was built was getting hard to work on so I put the lot into a metal enclosure..


I am planning on adding a 'wall' down the middle of the box to separate the electronics from the half that has water pumping round it, just in case :)

To test a theory about using Litz wire for the work coil I obtained some of these...

Polypropylene capacitor
1uF, 1500V Polypropylene capacitors.  Manufactured by ICW Ltd. I bolted three together to make 3uF...
Very nice.

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